Greg,
Drove by your place when you were getting the beast started. Looks like you had lots of help!
Congrats, it's so fun to get a project to start the first time. Looks like great work.
Richard
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6x6 Power Wagon Project
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Thanks Andy, I'm doing my best. This is my second restoration of a big
Dodge, and I learned a few things the first time, 30 years ago!
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Glad to hear your success story. Looks like your doing good work.
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Thanks Greg,
Yep, I actually moved it under it's own power last night. That is the first time in 25 years since it has moved under it's own power and almost exactly three years since I have owned it. Now fiddling with tuning it and fixing the toe-in so I can drive it around. Can't wait... :)
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Clark, I saw that you got your PW running as well. Congratulations!
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Got the engine running!
Yesterday was a very good day. The boys and I spent the morning prepping the engine and setting up a temporary ignition system. Then we primed the oil system using a 5/16" hex rod and a drill motor to spin up the oil pump. We got pressure almost right away, around 60 psi. Then we filled the cooling system, and made sure there was gas in the carburetor. For the initial start-up I was using the original spark plug wires, which tested out okay. The new spark plug wires were cut to length and installed after I knew where the distributor was going to end up (for timing).
A few friends came buy around 1:00p to watch the lift off. The engine wanted to run right away, but I wasn't sure how much choke to give it. After a couple tries I realized I had flooded the engine, so I opened the carb and she fired right up. We ran the engine at 2100-2400 rpm to break in the cam. After about 10 minutes before we noticed an overheating problem and we shut things down. We checked a couple things, but there were no obvious problems. We drained the coolant (which was very clean), pulled out the thermostat (the original, untested one), and fired it back up. Another 10 minutes later we were running hot again, so we shut it down. The cam was good and broken in by now.
During this time we set the ignition timing to 8-10 deg BTDC and checked the dwell, which was running at 30 deg - the spec for this engine is 35 deg. We noticed that cylinders 1 and 2 were running a little cool, so we swapped the old wires around and they perked back up, so I was glad to have the new set ready to install.
As for the engine overheating, we figure the problem is running a 16" flex fan without a shroud. The flex fan pulls less air as the engine speeds up, and the lack of a shroud makes the fan that much more inefficient. Making a new shroud shouldn't be a big deal. Last night I tested the old thermostat. It's set for 180 deg, but it didn't start to open till 200 deg. Time for a new one.
Now that we have passed this happy milestone, the chassis is virtually complete. It's time to start diving into bodywork, which is not my strong suit. But I'm looking forward to it, and we've already made some progress. My hope is to have the cab and front clip installed by September, and start putting some miles on the beast. Then we take on the bed and lift mechanism.
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Would love to be there! But Canada has me frozen in. Hope she purrs like a flathead 😮
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Engine Start-up, T minus 4 days and counting
I'm getting the last bits together to fire up the engine this Saturday. I've invited a few friends over to either celebrate or commiserate the event. If any of you local guys want to come over to watch, let me know. I'm aiming to flip the switches around 1:00p Saturday.
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It's those milestones that keep us going! Looking forward to the next progress report!
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Progress
Over the last week we've gotten a lot of things wrapped up on the chassis. Here's a quick list of recent progress:
Welded in the gusset for the clutch master cylinder bracket - it's much stiffer now
Found and installed the upper radiator hose
Installed the starter
Installed the carburetor
Primed the fuel line, fuel pump, and carburetor
Cleaned, painted and installed the air filter housing
Installed the PCV system
Painted the radiator frame and installed the radiator
Rebuilt, installed and painted the driveshafts
Installed temporary spark plug wires - tested out okay
Installed temporary exhaust system - scavenged from a 74 D200 w/318
After I primed the fuel line I found a tiny leak in the carburetor. It's coming from one of the plugs in the float body casting. It doesn't drip, but it's always a little damp. I'll have to see if there's an easy way to reset the plug, or take it to a carburetor shop to have them fix it.
I was at a friend's to look for some cab parts and stumbled (literally) over a gas pedal bracket from a 60's Dodge pickup that I may be able to use on this project. I uses a cable to connect to the carburetor, so it 'should' be easy to adapt it to the stock PW gas pedal and cab.
When I was checking out the pillow block I found something unexpected. The yokes and the shaft are splined so that it is not possible to align them 'in-phase'. At first I though one of the yokes might be a replacement, but looking at the splines they are identical. I also noticed that the cotter pin holes are drilled at 90 deg to each other, so even if you could align the yokes, you would not be able to install one of the cotter pins. This truck was made in late 1944, so I don't know if this is a change that was made during production, but it clearly appears to be intentional. Maybe having the 2 driveshafts in-phase to each other created extra vibration, so they changed the pillow block. At any rate, the yokes are 90 deg to each other, and that's that.
Next things to happen are buy a battery and cables to run to the starter and chassis, and build a simple electrical system to control the starter solenoid and ignition circuits. I also want to find the right size hexagonal rod to prime the oil pump and oil galleys before we fire up the engine. We used a lot of assembly lube when we built the engine, but it's been sitting for 2+ years, and an ounce of prevention....
If things go according to plan we hope to fire up the engine on April 4th.
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3 years down, probably 2 more to go!Nice!! You'll be done in no time!
It's an illusion. The original 7 blade fan was 18" in diameter and tagged the pump shaft pretty good, so I went with a 16" flex fan. The smaller fan also give more room to run the lower radiator hose.Looks like your fan blade is going to contact your pulley bolt? Or is it an optical illusion?
I've wanted to try a flex fan to see if it would help reduce the engine load, we'll see how it performs. I may have to build a shroud around the fan to help pull the air through the radiator, but I'll test it this way to see if it's necessary.
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Looks like your fan blade is going to contact your pulley bolt? Or is it an optical illusion?
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