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The "Hulk": Ugly green truck to Juneau??

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  • oldndcctrucks
    replied
    I got the front driveshaft, which was in the bed of the truck when I bought it, re-installed with two new clamp kits from NAPA. The clamps seemed short, so I was cautious tightening the bolts.

    I also got the front diff oil changed. The parts inside looked nice, but the oil was thick as honey. There was a lot of very dark sediment in the bottom. I also installed a magnet on the diff cover fill plug.

    Leave a comment:


  • oldndcctrucks
    replied
    I ran into a problem the other day, as noted in a separate thread, "1973 W200 T-205 transfer case support rod???" on this site:
    https://powerwagonadvertiser.com/for...se-support-rod

    "Well, I cut the “bubba rod” and now the transfer case shift lever in the cab shakes like crazy when accelerating; obviously a bandaid fix.

    I have determined the complete situation:

    1. When the transfer case input and output yokes are no longer "in phase" (lined up), shaking occurs.
    2. Yokes being "out of phase" is caused by transfer case operation in LOW.
    3. The yokes are placed back "in phase" easily by setting the parking brake, placing both the transmission and the transfer case in N neutral, and rotating the jack shaft between the two cases by hand, then placing the transfer case back into 2H.
    4. The Bubba rod was a bandaid which masked the problem.

    I found this exact situation with my truck; the yokes were about 90 degrees out-of-phase; performing the above action proved the problem with an immediate test-drive, which resulted in the transfer case shifter not shaking even a little.

    I found this explanation and solution at the "Sweptline.ORG '61-'71 Dodge Sweptline Truck Online Community" site:

    "
    Transfer Case Lever Shaking

    Post by JohnB » Mon Sep 22, 2014 3:37 am

    Got a chance to drive my W200 down about 20 miles of dirt road so I put in 4WD {High and Low range} to slosh some lubricant around the front diff. After putting the transfer case back in 2WD and driving on the pavement, I noticed the transfer case lever shakes back and forth quite a bit when starting out from a standing stop. Just shakes until the truck gets going and doesnt do it in any other gear while upshifting. Any ideas? Loose mounting bracket bolts? universals need grease? something else?

    John
    User avatar
    digdoug Sweptline.ORG Pioneer
    Posts:
    2851 Joined: Wed Dec 31, 1969 6:00 pm Location: Genesee,Id. Re: Transfer Case Lever Shaking
    Post by digdoug » Tue Sep 23, 2014 7:28 pm
    That is the downfall of divorced transfer cases. When you drive it in low range it messes up the phasing between the jack shaft and rear shaft.
    Just put the tc and tranny in neutral ,set the parking break,crawl under and line up the yokes of the two shafts.Put them back in gear and recheck to be sure the jack shaft is still in phase. "





    LINK: http://www.sweptline.org/forums/viewtopic.php?t=36820

    I am providing this info for continuity of the story and information.

    Leave a comment:


  • oldndcctrucks
    replied
    The rear bumper is coming along:
    90.jpg

    89.jpg

    I'm using 2" x 5" x .125" rectangle tube with 3/8" frame brackets and a
    2 1/2" x 3 1/2" x 1/4" angle stiffener; 1/2" grade 5 bolts with 3/16"
    opposite side backing plates where it bolts to the frame.

    I used 1/4 sections of 4" steel pipe for the ends.

    Leave a comment:


  • oldndcctrucks
    replied
    I will try again:

    On a different note:

    Since purchasing the truck, I have been unable to lock the cab due to door lock failures caused by broken plastic operating rod clips.

    Last weekend I finally got around to replacing the clips and getting the locks working. While doing that, I took off all the inside panels
    and cleaned out the bottoms of the doors:
    84.jpg
    This is from the front passenger door.
    When I was done with all four doors, I had more than a gallon of dirt and debris in a bucket.

    Also, I got a parts bag full of cigarette butts:

    85.jpg
    If some assembly line worker is looking at this, he's probably laughing his *** off....

    And finally, a REAL TREAT:

    87.jpg

    88.jpg
    This appears to be the original build sheet! Having it drop out at my feet really made my day



    Leave a comment:


  • oldndcctrucks
    replied
    I am having a REAL problem with posting pictures to this site.

    The post just previous is showing pictures other than what I inserted, and other than what is shown while in "edit" mode.

    All of the four images I downloaded and tried to post are less than 95 kb.

    ???

    Leave a comment:


  • oldndcctrucks
    replied
    On a different note:

    Since purchasing the truck, I have been unable to lock the cab due to door lock failures caused by broken plastic operating rod clips.

    Last weekend I finally got around to replacing the clips and getting the locks working. While doing that, I took off all the inside panels
    and cleaned out the bottoms of the doors:
    84.jpg
    This is from the front passenger door.
    When I was done with all four doors, I had more than a gallon of dirt and debris in a bucket.

    Also, I got a parts bag full of cigarette butts:
    85.jpg
    If some assembly line worker is looking at this, he's probably laughing his *** off....

    And finally, a REAL TREAT:
    87.jpg

    88.jpg
    This appears to be the original build sheet! Having it drop out at my feet really made my day

    Leave a comment:


  • oldndcctrucks
    replied
    Because I can hear it.

    I looked into it the other day- there is a new gasket/installer failure at cylinder 2 between the head and the manifold. This was a FelPro set, so either I screwed up the install or there is a mating surfaces flatness issue. I cleaned both head and manifold surfaces and inspected for cracks, but I don't have a machinists' straight edge, so I couldn't check the surfaces properly.

    I will have to pull the manifold again.

    Leave a comment:


  • KRB64
    replied
    "There is either an exhaust leak or possibly a burned exhaust valve on the passenger side"

    What makes you think that?

    Leave a comment:


  • oldndcctrucks
    replied
    Took the old beast for a test drive and there was considerably more low-end power, as well as more power at highway speed (55-60 mph).

    I know that it's easy to believe that kind of thing after doing a big job, but it seems very apparent that the old mufflers were probably rusted and restrictive, as well as the new, bigger, shorter pipes letting the engine breathe a lot better.

    It wasn't really any quieter, which I thought it might be with new "Quiet Flow" mufflers, but I can live with it I think.

    There is either an exhaust leak or possibly a burned exhaust valve on the passenger side; this is the side that had no coolant flow and I had driven the truck several miles over several short trips before correcting that.

    A thorough external inspection is next.

    Leave a comment:


  • oldndcctrucks
    replied
    I have just about finished the new exhaust.

    I installed 2 1/2", replacing 2":

    79.jpg

    What can't be seen is the old pipes were crushed about 10% - 15% at every bend due to the bender used.

    I don't have a bender, so I bought a kit:
    41PhZE+pS8L_pipe kit_edit.jpg


    AMAZON, Speedway, $149

    I can attest that the parts I received had very little crush; I'm very happy with the quality of this kit. Also, the couplings were a nice
    tight fit.

    I used all the straight pieces as well as all the 90's, plus one U cut into two pieces for two more 90's, as well as one 45.

    I also used two flex couplings; while not factory, I feel they will help prevent manifold gasket failure by reducing torque
    applied to the manifold by the long, heavy pipes while driving. Additionally, they may reduce felt and heard vibrations in the cab.
    They are located just after the 90 bends, after the manifolds.
    51eFLLlNlsL__SX522__flex coupling.jpg
    AMAZON, Remarkable Power, $12.34 each
    75.jpg

    For small bends and bends not exactly 45 or 90, I notched, bent, and welded:
    76.jpg

    77.jpg

    78.jpg
    The notch and weld method makes the pipes ugly, but I don't really care. I used a MillerMatic 211 machine.
    walker muffler.png

    I used two Walker stainless steel mufflers, #21337, $45.85 each at AMAZON

    This is what I replaced:
    73.jpg

    74.jpg
    Note the large number of stainless baling wire hangers; also the taillight wiring lying on the pipes.

    The new exhaust exits out the passenger side in front of the rear tire; I now have room for the new in-frame
    gas tank I intend to install, as both pipes hang on the passenger side. I used copper anti-seize on all the
    non-welded joints, the manifold flare couplings, and all the bolts. Also, the ahead-of-tire exit means
    no interference with the spare tire in the rear under the bed. Lastly, I painted all the non-stainless pipes
    with flat black hi-temp spray paint; these pipes will start rusting immediately (as happened when it rained
    on them last week).

    81.jpg

    83.jpg


    82.jpg
    I installed a piece of 14 gauge aluminum above the mufflers and under the rear of the cab to hopefully
    reduce heat and noise at that location.
    Attached Files
    Last edited by oldndcctrucks; 03-03-2019, 09:57 AM.

    Leave a comment:


  • KRB64
    replied
    Yea, a common weak leak. Look at most ammeter gauges in the dash and they are misshapen due to heat.

    Here's another old popular write-up:
    http://www.madelectrical.com/electri...p-gauges.shtml

    I understand why they use/suggest fusible links but I'm like you, not good for field fixes. They can fail and not even show it. I've converted most of mine in my '92 CTD.

    Leave a comment:


  • oldndcctrucks
    replied
    Suggested upgrades noted in the web article referenced above:

    http://madelectrical.com/electricalt...-gauges2.shtml

    There are a couple of things I would do differently:

    1. I would pass the new wires through a new hole and bushing in the firewall instead of through the existing plugs- I personally don’t like the restriction of the plug by a continuous wire, and it will be less work and less danger to existing wires by not drilling through the plugs.

    2. I would not install new fusible links; true, using them eliminates the extra points of contact compared to using fuses, but fusible links require extra tools to replace and are harder to remedy when burned “in the field”.

    Otherwise, that is a GREAT article! I had no idea the electrical system was that weak...!

    Leave a comment:


  • oldndcctrucks
    replied
    That’s GOOD STUFF thanks for the link!

    Leave a comment:


  • 712edf
    replied
    This is a good write-up on the factory Dodge ammeter.

    https://ramchargercentral.com/techni...ted-solutions/

    Bucky

    Leave a comment:


  • oldndcctrucks
    replied
    So I got the two adjustable voltage regulators today.

    They are TRANSPO-CN brand; a subsidiary of WAI International. Probably Chinese (go figure).
    I got them on eBay for $17 each plus some shipping.

    67.jpg

    69.jpg

    Note that factory regulators are not adjustable.

    The first one stabilized at 14.08 volts; unmounted, just plugged in with a jumper connecting the case to ground,
    with the dial on the back turned all the way down. Connecting a jumper from the output stud terminal on the
    alternator to the red ignition wire on the regulator plug brought the voltage down to no output (dial still turned
    all the way down) and the regulator was more adjustable. That is to say, the voltage out of the alternator was
    below the battery voltage, but came up to above battery voltage with adjustment of the dial on the back.

    The second stabilized at 13.7 volts, without the jumper from the input plug to the alternator output.

    The factory manual states that the voltage at the moderate temperature I am in should be 13.8 volts.

    I am running the second one, mounted and no jumpers, with the dial turned all the way down.

    If I have more but minor trouble, I will install a local relay that picks up with ignition ON” which will connect the
    alternator output to the red wire regulator input (ignition).

    These tests were with the original 65 amp alternator; I will test the 78 amp unit soon.

    *******************

    There is chatter on the interweb that the ammeter in the gage cluster is prone to smoking; I attribute this to
    under-sized wires (factory is only #10 which is normally rated for 30 amps in common building wiring). Continuous
    current at alternator max is bad. If I install the 78-amp unit, that’s 10% more; with a camper and it’s loads, and
    headlights at night, the ammeter will be running hot.

    So I will try paralleling the #10 alternator output wire with a #14. This should be enough resistance to still see
    movement on the ammeter but allow about 33% of the current to bypass the ammeter circuit. Of course, if the
    original circuit fails open, then all 78 amps would be pushed through a 15 amp wire; I will probably install a fuse.

    Leave a comment:

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